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U.S. Department of Energy
Office of Scientific and Technical Information

Multi-pattern low-tension demonstration flood, Big Muddy Field. Progress report, October-December 1983

Technical Report ·
OSTI ID:5362808
Polymer injection continued through the fourth quarter of 1983, bringing the total polymer-pusher slug size to 834,600 barrels. The average injection rate for the quarter was 1746 BPD compared to the third quarter rate of 1707 BPD. During December, the injection plant was down for 1-1/2 days due to a major power failure. Oil sales averaged 212 BOPD, 217 BOPD and 218 BOPD for October, November and December, respectively. The major power failure in December resulted in downtime for all producing wells. Cumulative project production is 149,287 barrels of oil as of December 31, 1983. Sulfonate production was observed in all producing wells with Well 88 showing the highest level (1875 ppM). Most other wells were 100 ppM or less in sulfonate. De-bugging tests of the auxiliary treating facility were still conducted during the quarter; however, the facility was fully operational. No major treating problems have occurred. 6 figures, 4 tables.
Research Organization:
Conoco, Inc., Casper, WY (USA)
DOE Contract Number:
AC03-78SF01424
OSTI ID:
5362808
Report Number(s):
DOE/SF/01424-T3; ON: DE84005660
Country of Publication:
United States
Language:
English