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Title: Quarterly review of 241-SY-101 mixer pump data: January - March 1999

Technical Report ·
DOI:https://doi.org/10.2172/797495· OSTI ID:797495

This report presents data obtained on 241-SY-101 pump performance. The period covered is January 1 through March 31, 1999. During the quarter: There were changes in pumping parameters. Both the pump volute pressure and amperage decreased during the quarter. It is not clear whether this was due to changes in waste properties (due to less solids or more entrained gas) or due to degradation of the pump. There was an indication of a 7.5-inch increase in the waste level at riser 1 A, and an average growth rate of 0.082 inches per day. There was an indication of a 5.7-inch increase in the waste level at riser 1C. This riser was flushed with water several times, which would lower the level of the crust at this location. Gases continued to be released at less than the pre-pump installation baseline rate, indicating a decrease in the gas generation rate, or an increase in gas retention, or both. The release rate was about 78 percent of the rate in the previous few quarters, and only 34 percent of the generation rate calculated prior to mixer pump installation in 1993. Key controls exist for waste temperature, gas concentration, pump parameters, and long-term waste behavior associated with the safe operation of the mixer pump that mitigates the buoyant displacement gas release event behavior of 241-SY-101. Table 1-1 compares the key controls and the current state of the waste as of March 3 1. 1999. The pump was run 28 times between January 1 and March 31, 1999. All of the pump runs were intended to be normal 25-minute, 1000-rpm excavation runs performed to mix the waste and release gas. Because of the pump oil often reached the high temperature alarm setpoint of 190 F, many of the runs were shortened (by as many as 8 minutes). This phenomenon was identified in November 1998, but got progressively worse over the quarter. The pump schedule was nominally three runs per week. However, core sampling activities interrupted the usual pump schedule several times during the quarter, resulting in less pump runs than normal. There is evidence that the pump is not operating the same as it has in previous years. Pump power and volute pressure have both been reduced. It is not clear whether this is a result of pump degradation or whether the fluid parameters of the waste have changed (less solids or more entrained gas).

Research Organization:
LMHC (US)
Sponsoring Organization:
ENVIRONMENTAL MANAGEMENT (US)
DOE Contract Number:
AC06-96RL13200
OSTI ID:
797495
Report Number(s):
HNF-4511, Rev.0; TRN: US0201928
Resource Relation:
Other Information: PBD: 22 Jul 1999
Country of Publication:
United States
Language:
English