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Title: Results of Performance Tests Performed on the John Watts WW Casing Connection on 7" Pipe

Technical Report ·
DOI:https://doi.org/10.2172/769641· OSTI ID:769641

Stress Engineering Services (SES) was contracted by Mr. John Watts to test his ''WW'' threaded connection developed for oilfield oil and gas service. This work was a continuation of testing performed by SES as reported in August of 1999. The connection design tested was identified as ''WW''. The samples were all integral (no coupled connections) and contained a wedge thread form with 90{sup o} flank angles relative to the pipe centerline. The wedge thread form is a variable width thread that primarily engages on the flanks. This thread form provides very high torque capacity and good stabbing ability and makeup. The test procedure selected for one of the samples was the newly written ISO 13679 procedure for full scale testing of casing and tubing connections, which is currently going through the ISO acceptance process. The ISO procedure requires a variety of tests that includes makeup/breakout testing, internal gas sealability/external water sealability testing with axial tension, axial compression, bending, internal gas thermal cycle tests and limit load (failure) tests. This test procedure was performed with one sample. Four samples were tested to failure. Table 1 contains a summary of the tasks performed by SES. The project started with the delivery of test samples by Mr. Watts. Pipe from the previous round of tests was used for the new samples. Figure 1 shows the structural and sealing results relative to the pipe body. Sample 1 was used to determine the torque capacity of the connection. Torque was applied to the capacity of SES's equipment which was 28,424 ft-lbs. From this, an initial recommended torque range of 7,200 to 8,800 ft-lbs. was selected. The sample was disassembled and while there was no galling observed in the threads, the end of the pin had collapsed inward. Sample 2 received three makeups. Breakouts 1 and 2 also had collapsing of the pin end, with no thread galling. From these make/breaks, it was decided to reduce the amount of lubricant applied to the connection by applying it to the box or pin only and reducing the amount applied. Samples 3 and 4 received one makeup only. Sample 5 initially received two make/breaks to test for galling resistance before final makeup, No galling was observed. Later, three additional make/breaks were performed with no pin end collapse and galling over 1/2 a thread occurring on one of the breakouts. During the make/break tests, the stabbing and hand tight makeup of the WW connection was found to be very easy and trouble free. There was no tendency to crossthread, even when stabbed at an angle, and it screwed together very smoothly up to hand tight. During power tight makeup, there was no heat generated in the box (as checked by hand contact) and no jerkiness associated with any of the makeups or breakouts. Sample 2 was tested in pure compression. The maximum load obtained was 1,051 kips and the connection was beginning to significantly deform as the sample buckled. Actual pipe yield was 1,226 kips. Sample 3 was capped-end pressure tested to failure. The capped-end yield pressure of the pipe was 16,572 psi and the sample began to leak at 12,000 psi. Sample 4 was tested in pure tension. The maximum load obtained was 978 kips and the connection failed by fracture at the pin critical section. Actual pipe yield was 1,226 kips. Sample 5 was tested in combined tension/compression and internal gas pressure. The sample was assembled, setup and tested four times. The first time was with a torque of 7,298 ft-lbs and the connection leaked halfway to ISO Load Point 2 with loads of 693 kips and 4,312 psi. The second time the torque was increased to 14,488 ft-lbs and a leak occurred at 849 kips and 9,400 psi, which was ISO Load Point 2. The third time the makeup torque was again increased, to 20,456 ft-lbs, and a leak occurred at 716 kips and 11,342 psi, ISO Load Point 4. The fourth test was with the same torque as before, 20,617 ft-lbs, and the connection successfully tested up to load step 56, ISO Load Point 6 (second round) before leaking at 354 kips and 11,876 psi. At this point, time and funds prevented additional testing to be performed.

Research Organization:
John D. Watts, Houston, TX
Sponsoring Organization:
USDOE
DOE Contract Number:
FG01-95EE15608
OSTI ID:
769641
Country of Publication:
United States
Language:
English