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Title: Blowout control: Response, intervention and management; Part 8

Journal Article · · World Oil; (United States)
OSTI ID:7194124
 [1];  [2]
  1. John Wright Co., Houston, TX (United States)
  2. CNG Producing Co., New Orleans, LA (United States)

A fourth gunk squeeze was successful in sealing off annuli behind 2 7/8-in. tubing located in CNG Producing Co.'s South Timbalier 76 Well F-1. This allowed bullheading gas back into the Big A sands with 18.5-ppg mud and killing the underground blowout on Feb. 14, 1993. A 20-bbl cement plug was placed below 15,800 ft to permanently isolate A sands from the hole in the 2 7/8-inch. at 14,829 ft. A pressure-temperature log run on Feb. 19, 1993, confirmed that there was no longer any flow in the wellbore. The following case history outlines steps taken to kill this high-pressure, high-temperature (HPHT) well's underground blowout.

OSTI ID:
7194124
Journal Information:
World Oil; (United States), Vol. 215:7; ISSN 0043-8790
Country of Publication:
United States
Language:
English