Pipeline gas from coal-hydrogenation IGT Hydrogasification Process). Project 9000 quarterly report No. 5, July 1--September 30, 1977
Details are reported of a post-run inspection and cleanup conducted after Test 63. The annual plant turnaround was conducted. This turnaround period is required for routine maintenance, repairs, and installation of new equipment, all of which are necessary for successful plant operation. As such, the annual plant turnaround is an integral part of advancing pilot plant studies to provide data for a commercial/demonstration plant design. Current tests are aimed at acquiring data for a commercial/demonstration plant by conducting an extended run (No. 64) with Peabody No. 10 Mine bituminous coal at high carbon conversions. Eight and one-half days of self-sustained operation at coal conversions ranging from 72% to 97% occurred during Test 64. This was a major step toward achieving the immediate contract objective. An electrical power failure, caused by an equipment malfunction in Commonwealth Edison's main power supply to the plant, forced the termination of test No. 65 after only 9 tons of coal had been processed. A coal-flow model was designed and constructed to simulate the second-stage gasifier and steam-oxygen gasifier. This model was used to investigate how the fluidized bed is established in the steam-oxygen gasifier and the stability of the bed to process upsets. Results of tests with this model are presented. Engineering assistance was provided to ERDA-Major Facilities Program Management (MFPM) and Procon, Inc., in the design of a commercial/demonstration plant based on the HYGAS (registered trademark) Process. This report contains the computer-generated material balance data presented to them. A detailed comparison of the actual HYGAS reactor results vs. those predicted by a computer model simulation is presented.
- Research Organization:
- Institute of Gas Technology, Chicago, IL (USA)
- OSTI ID:
- 6944434
- Report Number(s):
- FE-2434-20
- Country of Publication:
- United States
- Language:
- English
Similar Records
Pipeline gas from coal-hydrogenation (IGT hydrogasification process). Project 9000 monthly status report, August 1--31, 1977
Pipeline gas from coal-hydrogenation (IGT hydrogasification process). Project 9000 monthly status report, September 1--September 30, 1977
Pipline gas from coal-hydrogenation (IGT Hydrogasification Process). Project 9000 monthly status report, July 1--July 31, 1977
Technical Report
·
Sat Oct 01 00:00:00 EDT 1977
·
OSTI ID:5419224
Pipeline gas from coal-hydrogenation (IGT hydrogasification process). Project 9000 monthly status report, September 1--September 30, 1977
Technical Report
·
Mon Oct 31 23:00:00 EST 1977
·
OSTI ID:5172639
Pipline gas from coal-hydrogenation (IGT Hydrogasification Process). Project 9000 monthly status report, July 1--July 31, 1977
Technical Report
·
Thu Sep 01 00:00:00 EDT 1977
·
OSTI ID:7293907
Related Subjects
01 COAL, LIGNITE, AND PEAT
010404* -- Coal
Lignite
& Peat-- Gasification
010600 -- Coal
Lignite
& Peat-- Properties & Composition
CARBONACEOUS MATERIALS
CATALYSTS
CHEMICAL COMPOSITION
CHEMICAL REACTIONS
COAL
COAL GASIFICATION
COMPUTER CALCULATIONS
DATA
ENERGY SOURCES
FLUIDS
FOSSIL FUELS
FUEL GAS
FUELS
FUNCTIONAL MODELS
GAS FUELS
GASES
GASIFICATION
HYDROGEN COMPOUNDS
HYGAS PROCESS
INFORMATION
LIQUID WASTES
MAINTENANCE
MATERIAL BALANCE
METHANATION
OPERATION
OXYGEN COMPOUNDS
PILOT PLANTS
REPAIR
SIMULATION
SNG PROCESSES
THERMOCHEMICAL PROCESSES
WASTE WATER
WASTES
WATER
010404* -- Coal
Lignite
& Peat-- Gasification
010600 -- Coal
Lignite
& Peat-- Properties & Composition
CARBONACEOUS MATERIALS
CATALYSTS
CHEMICAL COMPOSITION
CHEMICAL REACTIONS
COAL
COAL GASIFICATION
COMPUTER CALCULATIONS
DATA
ENERGY SOURCES
FLUIDS
FOSSIL FUELS
FUEL GAS
FUELS
FUNCTIONAL MODELS
GAS FUELS
GASES
GASIFICATION
HYDROGEN COMPOUNDS
HYGAS PROCESS
INFORMATION
LIQUID WASTES
MAINTENANCE
MATERIAL BALANCE
METHANATION
OPERATION
OXYGEN COMPOUNDS
PILOT PLANTS
REPAIR
SIMULATION
SNG PROCESSES
THERMOCHEMICAL PROCESSES
WASTE WATER
WASTES
WATER