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Title: Operating experience with the Wellman-Lord/Allied Chemical flue gas desulfurization plant at northern Indiana Public Service Company's Dean H. Mitchell Station

Conference · · Proc., Annu. Meet., Air Pollut. Control Assoc.; (United States)
OSTI ID:6771892

During the 9/16/77-12/31/78 demonstration test period, FGD outages occurred on 315 out of 472 days because of corrosion of the booster fan's air foil blades resulting from accumulated fly ash, water, and ice in the fan housing and on the blades; high silica levels in the boiler; corrosion of the guillotine isolation damper resulting from fly ash buildup; and fluctuating steam pressure and flow to the FGD plant due to wet, poor-quality coal. Other problems included leaks in the absorber tray; plugging of the evaporator circulating pump driver during interruptions in the main steam supply; and a lower than expected purge dryer operating capacity. The booster fan problems have been resolved by revisions and additions to the fan design. The installation of a continuous silica analyzer and other modifications have effectively controlled the boiler silica problems. The damper was modified and the seals replaced with ones made of a more corrosion-resistant alloy, but the fly ash buildup problem persists. Higher-quality coal is now used so that boiler operation is no longer erratic.

Research Organization:
North. Indiana Public Serv. Co.
OSTI ID:
6771892
Report Number(s):
CONF-790634-
Journal Information:
Proc., Annu. Meet., Air Pollut. Control Assoc.; (United States), Vol. 79-31.7; Conference: 72. annual Air Pollution Control Association meeting, Cincinnati, OH, USA, 24 Jun 1979
Country of Publication:
United States
Language:
English