Performance analysis and optimization of the Prudhoe Bay miscible-gas project
- Arco Alaska Inc., Prudhoe Bay, AK (United States)
Because EOR oil response at Prudhoe Bay has been difficult to measure directly, a number of different types of field measurements have been made to evaluate the miscible-flood displacement efficiency. These measurements include water- and solvent-injection profiles, logging data from an observation well, and single-well tracer test (SWTT) data. Despite ambiguity in these data, the measurements support the simulation nd laboratory data and generally indicate that the Prudhoe Bay Miscible Gas Project (PBMGP) is performing well. The most useful EOR surveillance data have been the separator-gas-sample database, with {approx} 4,000 compositional analyses. Separator flash analysis and allocation programs use this data-base to infer EOR performance on the basis of produced solvent. Reservoir mechanisms that adversely affect the EOR process efficiency have been identified. The project has exceeded initial expectations in terms of solvent retained within the reservoir, which has favorable implications for solvent sweep efficiency. Procedures have been developed to use the field and simulation data to determine how the solvent should be allocated to the existing patterns and when the project should be expanded into new areas. these procedures are designed to maximize the value of the PBMGP.
- Sponsoring Organization:
- USDOE
- OSTI ID:
- 49260
- Journal Information:
- SPE Reservoir Engineering, Journal Name: SPE Reservoir Engineering Journal Issue: 2 Vol. 10; ISSN 0885-9248; ISSN SREEEF
- Country of Publication:
- United States
- Language:
- English
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