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Title: Novel fracture technology proves marginal Viking prospect economic, part II: Well clean-up, flowback and testing

Conference ·
OSTI ID:457330

Having completed both fracture treatments as discussed in a companion paper, this paper continues on to describe the post fracture shut-in, clean-up and well testing operations that took place on the Viking Wx exploration well 49/17-12. These operations involved the removal of Resin Coated Proppant (RCP) from the wellbore, via Coiled Tubing (CT), through the use of a specially designed jetting nozzle. The RCP pack stability at a concentration of 3.0 lb/ft{sup 2} (as per planned design) had already been tested in a flowback cell. The use of a Surface Read-Out (SRO) gauge, combined with gas, water and proppant flow rates as well as the viscosity of fracturing fluids returns, enabled real time calculation of the drag forces, on the proppant pack, during clean-up. The flow rate, in the field, was controlled such that the calculated drag forces remained below those observed in the laboratory. Following the clean-up a flow and build-up test was conducted, to evaluate the fracture half length and fracture conductivity, from which a Pseudo-radial skin was calculated. The Non-Darcy effects in the fracture were also evaluated, and finally the short term and long term well deliverabilities were assessed.

OSTI ID:
457330
Report Number(s):
CONF-961003-; TRN: 96:006576-0052
Resource Relation:
Conference: 71. annual technical conference and exhibition of the Society of Petroleum Engineers, Denver, CO (United States), 6-9 Oct 1996; Other Information: PBD: 1996; Related Information: Is Part Of 1996 SPE annual technical conference and exhibition: Drilling and completion; PB: 944 p.
Country of Publication:
United States
Language:
English