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Title: Maximize the benefit of SNCR: Combine SNCR with combustion optimization and achieve 50% NOx reduction from a low NOx burner baseline

Conference ·
OSTI ID:20034357

PECO Energy Company operates one coal fired boiler at its Cromby Generating Facility. Cromby Unit 1 is a B and W front fired unit rated at 160 MW. The units boiler has been retrofitted with low NOx burners and overfire air ports. Due to NOx allowance pricing, PECO began evaluating options for reducing Cromby's NOx emissions. SNCR was evaluated at the best option for the plant even though the furnace exit temperatures and CO were high at practical injection locations. RJM Corporation, a Fuel Tech NOxOUT{trademark} Implementer, was selected to supply the system because of their extensive experience in solving combustion problems and applying NOxOUT SNCR systems on utility boilers. In order to reduce emissions during the 1999 NOx season, the deadline for an operational system was set at June 2nd. The project was issued on a fast track schedule starting February 2, 1999. The boiler was started up on June 2 on schedule after a six week maintenance outage. The project's 25% NOx reduction target was achieved after two weeks of combustion optimization. Combustion optimization was followed by NOxOUT A reagent injection system optimization which resulted in a 50% combined NOx reduction. Other benefits included a reduction in CO to less than 100 ppm and a 33% reduction in LOI.

Research Organization:
PECO Energy Co. (US)
OSTI ID:
20034357
Resource Relation:
Conference: 25th International Technical Conference on Coal Utilization and Fuel Systems, Clearwater, FL (US), 03/06/2000--03/09/2000; Other Information: PBD: 2000; Related Information: In: 25th international technical conference on coal utilization and fuel systems: Proceedings, by Sakkestad, B.A. [ed.], 969 pages.
Country of Publication:
United States
Language:
English