Skip to main content
U.S. Department of Energy
Office of Scientific and Technical Information

Naphthalene hydrogenation over Pt/Al{sub 2}O{sub 3} catalyst in a trickle bed reactor

Journal Article · · Industrial and Engineering Chemistry Research
;  [1]
  1. National Cheng Kung Univ., Tainan (Taiwan, Province of China). Dept. of Chemical Engineering

The biaromatic compound naphthalene dissolved in different volatile solvents has been hydrogenated over Pt/Al{sub 2}O{sub 3} catalyst in a trickle bed reactor. The activity and selectivity have been investigated with various hydrogen and feed flow rates at 513 K and 5.17 MPa. The effects of partial liquid evaporization and wetting efficiency of catalyst particles o the performance of a trickle-bed reactor were studied. Experimental results and parameters calculated from the reactor model indicated that neglecting the wetting efficiency would lead to a misleading conclusion in reaction kinetics. High volatilities of feedstocks, high gas flow rate, and low liquid flow rate decrease wetting efficiencies of catalyst particles. The activity of naphthalene hydrogenation increased with increasing wetting efficiency, and the selectivity of cis-decalin decreased with increasing volatility of solvent.

Sponsoring Organization:
USDOE
OSTI ID:
178395
Journal Information:
Industrial and Engineering Chemistry Research, Journal Name: Industrial and Engineering Chemistry Research Journal Issue: 7 Vol. 34; ISSN IECRED; ISSN 0888-5885
Country of Publication:
United States
Language:
English

Similar Records

Kinetic study of naphthalene hydrogenation over Pt/Al{sub 2}O{sub 3} catalyst
Journal Article · Fri Mar 31 23:00:00 EST 1995 · Industrial and Engineering Chemistry Research · OSTI ID:63148

Modeling of trickle-bed reactors at low liquid flow rates
Thesis/Dissertation · Wed Dec 31 23:00:00 EST 1986 · OSTI ID:7162792

Over-all catalyst effectiveness factors (g/sub o/) in trickle-bed reactors
Journal Article · Tue May 01 00:00:00 EDT 1979 · AIChE J.; (United States) · OSTI ID:6682752