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U.S. Department of Energy
Office of Scientific and Technical Information

LIFAC Sorbent Injection Desulfurization Demonstration Project. Quarterly report number 14, January--March, 1994

Technical Report ·
OSTI ID:10191163
The host site for the $22 million, three-phase project is Richmond Power and Light`s Whitewater Valley Unit No. 2 in Richmond, Indiana. The LIFAC technology uses upper-furnace limestone injection with patented humidification of the flue gas to remove 75--85% of the sulfur dioxide (SO{sub 2}) in the flue gas. During this report period (January--March 1994), long-term testing was initiated. The variable frequency drive was placed back in service, but failed again after only a few days of operation. The Unit No. 2 induced draft (ID) fan motor operates at maximum amperage during peak (65 MW) boiler load. LIFAC increases system pressure drop approximately 4.5 inches of water, causing additional loading on the fan motor. A variable frequency drive (VFD) was installed as a major component of the LIFAC system. The VFD interfaces with the ID fan motor by varying motor current as the pressure drop and flue gas volume change, making the fan more efficient and decreasing the stress on the motor. The VFD has failed several times causing boiler Unit No. 2 to trip. Since the VFD has become unreliable, the LIFAC team decided to perform a test on the ID fan motor with the bypass damper fully closed and the VFD disengaged. The objective of long-term testing is to evaluate the performance and operability of the LIFAC process over a long, continuous operation period. There were a total of two test periods during this quarter. Results are presented.
Research Organization:
LIFAC North America, Inc., Pittsburgh, PA (United States)
Sponsoring Organization:
USDOE, Washington, DC (United States)
DOE Contract Number:
FC22-91PC90548
OSTI ID:
10191163
Report Number(s):
DOE/PC/90548--T13; ON: DE95001952; BR: AZ0502050
Country of Publication:
United States
Language:
English