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Title: Thorough Chemical Decontamination with the MEDOC Process : Batch Treatment of Dismantled Pieces or Loop Treatment of Large Components Such as the BR3 Steam Generator and Pressurizer

Conference ·
OSTI ID:825825

The dismantling of the BR3-PWR reactor leads to the production of large masses of contaminated metallic pieces, including structural materials, primary pipings, tanks and heat exchangers. One of our main objectives is to demonstrate that we can minimize the volume of radioactive waste in an economical way, by the use of alternative waste routes, such as the clearance of materials after thorough decontamination. The SCKoCEN uses its own developed chemical decontamination process, so-called MEDOC (Metal Decontamination by Oxidation with Cerium), based on the use of cerium IV as strong oxidant in sulphuric acid with continuous regeneration using ozone. An industrial installation has been designed and constructed in close collaboration with Framatome-ANP (France). This installation started operation in September 1999 for the treatment of the metallic pieces arising from the dismantling of the BR3 reactor. Since then, more than 25 tons of contaminated material including primary pipes have been treated batchwise with success. 75 % of material could be directly cleared after treatment (Activity lower than 0.1 Bq/g for 60Co) and the other 25% free released after melting activity. The SCKoCEN performed in April 2002 the closed loop decontamination of the BR3 Steam Generator by connection of the MEDOC plant after few adaptations. The decontamination was done within 30 cycles in 3 weeks with consecutive steps like decontamination steps (injection of the solution into the SG) and regeneration steps with ozone. In total, 60 hours of decontamination at 70 C and 130 hours of regeneration were needed to reach the objectives. The tube bundle (600 m2) was attacked and about 10 {micro}m representing more than 41 kg of stainless steel and 2.06 GBq of 60Co was dissolved into the solution. The residual contamination measurements made directly into the water box are still going on, however it seems that the objective to reach the free release criteria after melting is achieved. The next decontamination operations of large components concern the primary pumps (*2) and the pressurizer and are foreseen in October 2002. The decontamination studies of large components take into account the technical aspects, the radiological and classical safety aspects, as well as the financial aspect.

Research Organization:
SCKoCEN, Belgian Nuclear Research Centre (BE); FRAMATOME-ANP, Tour Framatome, 92084 Paris La Defense Cedex (FR)
Sponsoring Organization:
none (US)
OSTI ID:
825825
Resource Relation:
Conference: Waste Management 2003 Symposium, Tucson, AZ (US), 02/23/2003--02/27/2003; Other Information: PBD: 25 Feb 2003
Country of Publication:
United States
Language:
English