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Title: Final report on Technical Demonstration and Economic Validation of Geothermally-Produced Electricity from Coproduced Water at Existing Oil/Gas Wells in Texas

The initial geothermal brine flow rate and temperature from the re-worked well were insufficient, after 2.5 days of flow testing, to justify advancing past Phase I of this project. The flow test was terminated less than 4 hours from the Phase I deadline for activity, and as such, additional flow tests of 2+ months may be undertaken in the future, without government support.
  1. Universal GeoPower LLC, Houston, TX (United States)
Publication Date:
OSTI Identifier:
Report Number(s):
Final 1.1
DOE Contract Number:
Resource Type:
Technical Report
Research Org:
Universal GeoPower LLC, Houston, TX (United States)
Sponsoring Org:
USDOE Office of Energy Efficiency and Renewable Energy (EERE), Geothermal Technologies Office (EE-4G)
Country of Publication:
United States
15 GEOTHERMAL ENERGY Co-produced geothermal brine