Abstract
The aim of this project was to optimize the Volvo AH10A245 engine design parameters for ethanol fuel with Beraid (Trade mark of the ignition improver manufactured by the Akzo Nobel Surface Chemistry AB). The method used was engine testing with variation of design, performance, and other functional parameters, which affect the engine thermodynamics, and exhaust gas composition. The first design parameter, which was tested and optimized was the compression ratio, which was optimized at the ratio of 23:1. In order to prevail the fuel spray impingement, which might affect the unburned or partially burned emissions (CO), the combustion chamber was redesigned to a straight-side wall bowl in piston. Furthermore, the injector position was optimized by means of lifting or descending it few millimeters. The best emission levels was achieved with the injector lift of 1.00 mm. The inlet air temperature was optimized for lower emissions by removing the intercooler thermostat. Injector nozzles with different cross section areas of holes were tested, and the 6 holes injector nozzles with smaller cross sectional area, compared with base nozzles, were selected. The engine performance was maintained for lower engine rated speed 2000 (instead of 2200 rpm for conventional engine) and lower intermediate speed
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Gjirja, S
[1]
- Chalmers Univ. of Technology, Gothenburg (Sweden). Dept. of Thermo- and Fluid Dynamics
Citation Formats
Gjirja, S.
Engine design optimization for running on ethanol with low emissions.
Sweden: N. p.,
1996.
Web.
Gjirja, S.
Engine design optimization for running on ethanol with low emissions.
Sweden.
Gjirja, S.
1996.
"Engine design optimization for running on ethanol with low emissions."
Sweden.
@misc{etde_378191,
title = {Engine design optimization for running on ethanol with low emissions}
author = {Gjirja, S}
abstractNote = {The aim of this project was to optimize the Volvo AH10A245 engine design parameters for ethanol fuel with Beraid (Trade mark of the ignition improver manufactured by the Akzo Nobel Surface Chemistry AB). The method used was engine testing with variation of design, performance, and other functional parameters, which affect the engine thermodynamics, and exhaust gas composition. The first design parameter, which was tested and optimized was the compression ratio, which was optimized at the ratio of 23:1. In order to prevail the fuel spray impingement, which might affect the unburned or partially burned emissions (CO), the combustion chamber was redesigned to a straight-side wall bowl in piston. Furthermore, the injector position was optimized by means of lifting or descending it few millimeters. The best emission levels was achieved with the injector lift of 1.00 mm. The inlet air temperature was optimized for lower emissions by removing the intercooler thermostat. Injector nozzles with different cross section areas of holes were tested, and the 6 holes injector nozzles with smaller cross sectional area, compared with base nozzles, were selected. The engine performance was maintained for lower engine rated speed 2000 (instead of 2200 rpm for conventional engine) and lower intermediate speed 1250 (instead of 1320 rpm for conventional engine). Such engine performance optimization was followed by the improved specific fuel consumption, and lower emissions compared with conventional speeds. The backpressure governor, desperately needed during the first phase of engine design optimization was, finally avoided. It can only be used as in the conventional diesel engine. 7 refs, 26 figs, 18 tabs, 7 appendices}
place = {Sweden}
year = {1996}
month = {May}
}
title = {Engine design optimization for running on ethanol with low emissions}
author = {Gjirja, S}
abstractNote = {The aim of this project was to optimize the Volvo AH10A245 engine design parameters for ethanol fuel with Beraid (Trade mark of the ignition improver manufactured by the Akzo Nobel Surface Chemistry AB). The method used was engine testing with variation of design, performance, and other functional parameters, which affect the engine thermodynamics, and exhaust gas composition. The first design parameter, which was tested and optimized was the compression ratio, which was optimized at the ratio of 23:1. In order to prevail the fuel spray impingement, which might affect the unburned or partially burned emissions (CO), the combustion chamber was redesigned to a straight-side wall bowl in piston. Furthermore, the injector position was optimized by means of lifting or descending it few millimeters. The best emission levels was achieved with the injector lift of 1.00 mm. The inlet air temperature was optimized for lower emissions by removing the intercooler thermostat. Injector nozzles with different cross section areas of holes were tested, and the 6 holes injector nozzles with smaller cross sectional area, compared with base nozzles, were selected. The engine performance was maintained for lower engine rated speed 2000 (instead of 2200 rpm for conventional engine) and lower intermediate speed 1250 (instead of 1320 rpm for conventional engine). Such engine performance optimization was followed by the improved specific fuel consumption, and lower emissions compared with conventional speeds. The backpressure governor, desperately needed during the first phase of engine design optimization was, finally avoided. It can only be used as in the conventional diesel engine. 7 refs, 26 figs, 18 tabs, 7 appendices}
place = {Sweden}
year = {1996}
month = {May}
}