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Fiscal 1999 international energy conservation model project. Report on result of demonstrative research concerning cement clinker cooling system; 1999 nendo kokusai energy shohi koritsuka nado model jigyo seika hokokusho. Cement clinker reikyaku sochi ni kakawaru jissho kenkyu

Abstract

For the purpose of reducing energy consumption and CO2 discharge in a cement plant in Indonesia, R and D was conducted on new clinker cooling system, high performance kiln combustion system, and technology for steady kiln operation and control, with the fiscal 1999 results reported. In the research on the optimum clinker cooling system, a new type clinker cooling system (CCS) was developed in which air beams are applied only to stationary grate rows, in an air beam type clinker cooling system where cooling air is fed to each block, with grate plates used as the air duct. This year, in an actual machine testing equipment (capacity 2,500 t/d), the whole heat recuperation area was modified for the CCS, with the operation started since February, 1999, aiming at the optimal clinker cooling effect and high heat recovery efficiency. The heat quantity for the entire system showed a decrease of 60 kcal/kg in the heat consumption rate through CCS modification, kiln burner adjustment, etc. So long as the demonstration plant is concerned, design of a new type burner and study/design for the kiln stabilization were nearly completed. (NEDO)
Authors:
"NONE"
Publication Date:
Mar 01, 2000
Product Type:
Technical Report
Report Number:
JP-NEDO-010016763
Resource Relation:
Other Information: PBD: Mar 2000
Subject:
32 ENERGY CONSERVATION, CONSUMPTION, AND UTILIZATION; ENERGY CONSUMPTION; ENERGY CONSERVATION; ENERGY EFFICIENCY; CEMENT INDUSTRY; INDONESIA; CARBON DIOXIDE; KILNS; COOLING SYSTEMS; HEAT RECOVERY; COMBUSTION CONTROL; BURNERS
OSTI ID:
20225468
Research Organizations:
New Energy and Industrial Technology Development Organization, Tokyo (Japan)
Country of Origin:
Japan
Language:
Japanese
Other Identifying Numbers:
TRN: JN0141062
Availability:
Available to ETDE participating countries only(see www.etde.org); commercial reproduction prohibited; OSTI as DE20225468
Submitting Site:
NEDO
Size:
186 pages
Announcement Date:

Citation Formats

Fiscal 1999 international energy conservation model project. Report on result of demonstrative research concerning cement clinker cooling system; 1999 nendo kokusai energy shohi koritsuka nado model jigyo seika hokokusho. Cement clinker reikyaku sochi ni kakawaru jissho kenkyu. Japan: N. p., 2000. Web.
Fiscal 1999 international energy conservation model project. Report on result of demonstrative research concerning cement clinker cooling system; 1999 nendo kokusai energy shohi koritsuka nado model jigyo seika hokokusho. Cement clinker reikyaku sochi ni kakawaru jissho kenkyu. Japan.
2000. "Fiscal 1999 international energy conservation model project. Report on result of demonstrative research concerning cement clinker cooling system; 1999 nendo kokusai energy shohi koritsuka nado model jigyo seika hokokusho. Cement clinker reikyaku sochi ni kakawaru jissho kenkyu." Japan.
@misc{etde_20225468,
title = {Fiscal 1999 international energy conservation model project. Report on result of demonstrative research concerning cement clinker cooling system; 1999 nendo kokusai energy shohi koritsuka nado model jigyo seika hokokusho. Cement clinker reikyaku sochi ni kakawaru jissho kenkyu}
abstractNote = {For the purpose of reducing energy consumption and CO2 discharge in a cement plant in Indonesia, R and D was conducted on new clinker cooling system, high performance kiln combustion system, and technology for steady kiln operation and control, with the fiscal 1999 results reported. In the research on the optimum clinker cooling system, a new type clinker cooling system (CCS) was developed in which air beams are applied only to stationary grate rows, in an air beam type clinker cooling system where cooling air is fed to each block, with grate plates used as the air duct. This year, in an actual machine testing equipment (capacity 2,500 t/d), the whole heat recuperation area was modified for the CCS, with the operation started since February, 1999, aiming at the optimal clinker cooling effect and high heat recovery efficiency. The heat quantity for the entire system showed a decrease of 60 kcal/kg in the heat consumption rate through CCS modification, kiln burner adjustment, etc. So long as the demonstration plant is concerned, design of a new type burner and study/design for the kiln stabilization were nearly completed. (NEDO)}
place = {Japan}
year = {2000}
month = {Mar}
}