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Development of a filter for dust separation from hot, untreated gases. Final report; Entwicklung eines Filters zur Staubabscheidung aus heissen, unbehandelten Pyrolysegasen. Abschlussbericht

Abstract

The final objective was the testing of suitable filter materials for the dust separation in untreated gases resulting from pyrolysis. For this purpose we chose an Inconell nonwoven with a structure similar to that of the cloth filter as well as a foam ceramics (ceramics as high temperature resistant filter material). The tests carried out proved that both filter materials are sufficiently stable for the type of application required (550deg C) as far as temperature is concerned. The corrosion susceptibility as the fibres were partially destroyed by condensated acids occuring at startup and shutdown. Due to the structure of the porous foam led to the impossibility of cleaning these elements completely after an operation period of 350 h. Effected clean gas measurements can only be used with certain restrictions as condensates from the pyrolysis gas filtered off in addition to the separated dust falsify the measuring values. After the Inconell nonwoven the clean gas concentration are between 126 mg/m{sup 3} (standard, dry) and 899 mg/m{sup 3} s.d. Similar particle concentrations were measured after the foam ceramics - between 187 mg/m{sup 3} s.d. and 791 mg/m{sup 3} s.d. At the entering of the combustion chamber the clean gas concentration should be  More>>
Authors:
Publication Date:
Nov 01, 1988
Product Type:
Miscellaneous
Report Number:
ETDE-mf-92784214
Reference Number:
SCA: 540120; PA: DE-92:002294; SN: 92000687142
Resource Relation:
Other Information: PBD: Nov 1988
Subject:
54 ENVIRONMENTAL SCIENCES; AIR FILTERS; PERFORMANCE TESTING; PYROLYTIC GASES; AIR POLLUTION CONTROL; MATERIALS; INCONEL 600; CERAMICS; MUNICIPAL WASTES; TEMPERATURE RANGE 0400-1000 K; FIBERS; PARTICULATES; 540120; CHEMICALS MONITORING AND TRANSPORT
OSTI ID:
10130613
Research Organizations:
Deutsche Babcock Anlagen AG, Krefeld (Germany); Bundesministerium fuer Forschung und Technologie, Bonn (Germany)
Country of Origin:
Germany
Language:
German
Other Identifying Numbers:
Other: ON: DE92784214; CNN: Contract BMFT 14405030; TRN: DE9202294
Availability:
OSTI; NTIS (US Sales Only)
Submitting Site:
DE
Size:
42 p.
Announcement Date:
Jul 04, 2005

Citation Formats

Ruther, G. Development of a filter for dust separation from hot, untreated gases. Final report; Entwicklung eines Filters zur Staubabscheidung aus heissen, unbehandelten Pyrolysegasen. Abschlussbericht. Germany: N. p., 1988. Web.
Ruther, G. Development of a filter for dust separation from hot, untreated gases. Final report; Entwicklung eines Filters zur Staubabscheidung aus heissen, unbehandelten Pyrolysegasen. Abschlussbericht. Germany.
Ruther, G. 1988. "Development of a filter for dust separation from hot, untreated gases. Final report; Entwicklung eines Filters zur Staubabscheidung aus heissen, unbehandelten Pyrolysegasen. Abschlussbericht." Germany.
@misc{etde_10130613,
title = {Development of a filter for dust separation from hot, untreated gases. Final report; Entwicklung eines Filters zur Staubabscheidung aus heissen, unbehandelten Pyrolysegasen. Abschlussbericht}
author = {Ruther, G}
abstractNote = {The final objective was the testing of suitable filter materials for the dust separation in untreated gases resulting from pyrolysis. For this purpose we chose an Inconell nonwoven with a structure similar to that of the cloth filter as well as a foam ceramics (ceramics as high temperature resistant filter material). The tests carried out proved that both filter materials are sufficiently stable for the type of application required (550deg C) as far as temperature is concerned. The corrosion susceptibility as the fibres were partially destroyed by condensated acids occuring at startup and shutdown. Due to the structure of the porous foam led to the impossibility of cleaning these elements completely after an operation period of 350 h. Effected clean gas measurements can only be used with certain restrictions as condensates from the pyrolysis gas filtered off in addition to the separated dust falsify the measuring values. After the Inconell nonwoven the clean gas concentration are between 126 mg/m{sup 3} (standard, dry) and 899 mg/m{sup 3} s.d. Similar particle concentrations were measured after the foam ceramics - between 187 mg/m{sup 3} s.d. and 791 mg/m{sup 3} s.d. At the entering of the combustion chamber the clean gas concentration should be leas than 100 mg/m{sup 3} s.d. to avoid installation of a second filter. A positive finding, however, is the little consumption of nitrogen for the pulse jet cleaning process. It is considerably lower than that for traditional cloth filters. (orig.) With 3 refs., 5 tabs., 12 figs. [Deutsch] Gesamtziel war die Erprobung geeigneter Filtermaterialien zur Entstaubung von unbehandelten Pyrolysegasen. Hierzu wurden ein Inconell-Faservlies, im Aufbau aehnlich einem Glasfaservlies, sowie eine Schaumkeramik (Keramik als hochtemperaturbestaendiges Filtermaterial) ausgesucht. Die durchgefuehrten Untersuchungen haben gezeigt, dass beide Filtermaterialien fuer den Anwendungsfall (550deg C) thermisch ausreichend stabil sind. Nachteilig wirkte sich die Korrosionsanfaelligkeit der Metallfasern aus, da durch An- und Abfahrvorgaenge kondensierte Saeuren die Fasern teilweise zerstoerten. Bedingt durch den Aufbau der poroesen Schaumkeramik zeigten diese Elemente ein Tiefenfiltrationsverhalten, was zur Folge hatte, dass diese Elemente nach einer Betriebsdauer von 350 h nicht mehr vollstaendig abzureinigen waren. Durchgefuehrte Reingaskonzentrationsmessungen sind bedingt verwertbar, da neben dem abgeschiedenen Staub abfiltrierte Kondensate aus dem Pyrolysegas die Messwerte verfaelschen. So wurden bei den Inconell-Geweben Reingaskonzentrationen zwischen 126 und 899 mg/m{sup 3} n.tr. erzielt, waehrend hinter dem Schaumkeramikfilter Schadstoffkonzentrationen (Staub und Kondensat) zwischen 187 und 791 mg/m{sup 3} n.tr. gemessen wurden. Als Reingasstaubgehalt vor der Brennkammer war jedoch ein Wert von < 100 mg/m{sup 3} n.tr. angestrebt worden, um auf ein nachgeschaltetes Filter zu verzichten. Positiv ist der geringe Stickstoffverbrauch zur Abreinigung mit Puls-Jet, der deutlich unterhalb des Verbrauchs traditioneller Gewebefilter liegt. (orig.) With 3 refs., 5 tabs., 12 figs.}
place = {Germany}
year = {1988}
month = {Nov}
}