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Title: Investigation into the failure cause of a double-acting, leading-edge-groove, tilting-pad thrust bearing. Final report, Feb-Aug 90

Technical Report ·
OSTI ID:5343911

This report describes the results of bench tests simulating operation and failure of a thrust bearing used in a gas turbine engine compressor development test rig. The bearing was a double acting, tilting pad with offset pivot, leading edge groove configuration using an AMS 4928 titanium collar and C18200 copper-chrome alloy pads with a No. 2 babbitt face. The bench tests successfully simulated the bearing failure and demonstrated a materials incompatibility. This was supported by visual examination, scanning electron microscopy and X-ray energy spectroscopy. A comparison of the bench test results to the compressor rig bearing failure is provided to support the report conclusions.

Research Organization:
Air Force Wright Research and Development Center, Wright-Patterson AFB, OH (United States)
OSTI ID:
5343911
Report Number(s):
AD-A-235613/7/XAB; WRDC-TR-90-2120
Country of Publication:
United States
Language:
English