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Title: Pilot Scale Operation and Testing of Syngas Chemical Looping For Hydrogen Production

Technical Report ·
DOI:https://doi.org/10.2172/1487263· OSTI ID:1487263

The Syngas Chemical looping (SCL) process provides efficient and economic means to utilize the abundant fossil reserve of coal. The main problem associated with coal utilization is the CO2 emissions resulting from its combustion. Even though CO2 regulation or carbon tax is currently not in place, its enforcement is expected in the near future. Such a greenhouse gas emission control, if adopted in current power plant systems, will drive the efficiency down and increase the cost of electricity, due to the energy and capital-intensive nature of current CO2 separation techniques. This highlights the need to develop technologies that present a solution to the rising cost of electricity in the future. The integrated gasification combined cycle (IGCC) presents an improvement to the above predicament, but it is capital intensive due to the extensive unit operations involved. The efficiency for a CO2 capture incorporated IGCC system is around ~32%, resulting in approximately 45% increase in cost of electricity. This is definitely a better path to traverse than the conventional pulverized coal (PC) power plants as it has improved economics and efficiencies accompanied by product flexibility. The SCL process advances the benefits even further when integrated with the IGCC process. The SCL process removes the expensive WGS system and CO2 separation columns, thereby saving on capital and operational expenses. This integration results in a 12 – 21% increase in efficiency accompanied by a reduction in cost of electricity by 15 – 28%, over conventional IGCC systems. Therefore, SCL process provides the best route to harness the energy from coal. The overall project objective was to construct and operate a syngas chemical looping pilot scale test unit at the NCCC. The project scope of work was divided into 3 phases. In Phase I, cold flow model studies using a 1:1 scale acrylic test unit constructed at Particulate Solids Research, Inc. (PSRI) was successfully completed confirming robust solid flow control is achievable in the non-mechanical system design. In Phase II, the high pressure, high temperature, chemical looping reactor was successfully designed with all necessary equipment and safety instrumentation/controls specified to allow for fabrication, site construction, and assembly to commence in Phase III. In Phase III, the SCL pilot plant was successfully assembled and all necessary functional checks and pre-startup safety reviews completed. During unit commission over the course of 200 hours of testing, operational issues were observed with premix burner used for system startup. With the grants awarded by the National Energy Laboratory (NETL) and the Ohio Development Services Agency (ODSA) under awards DE-FE0023915 and D-14-18, the SCL pilot unit underwent three auxiliary equipment modifications to resolve all of the startup operational issues encountered. The unit was successfully demonstrated with 300+hr continuous operation. Key results obtained include high syngas conversion of 97.95% with 16.03% oxygen carrier conversion in the moving bed reducer and >99% purity H2 produced from the moving bed oxidizer.

Research Organization:
The Ohio State Univ., Columbus, OH (United States)
Sponsoring Organization:
USDOE Office of Fossil Energy (FE)
Contributing Organization:
Babcock and Wilcox Company
DOE Contract Number:
FE0023915
OSTI ID:
1487263
Report Number(s):
DOE-OSU-FE-23915
Country of Publication:
United States
Language:
English