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Title: Mass Transfer And Hydraulic Testing Of The V-05 And V-10 Contactors With The Next Generation Solvent

Abstract

The Modular Caustic Side Solvent Extraction (CSSX) Unit (MCU) facility is actively pursuing the transition from the current BOBCalixC6 based solvent to the Next Generation Solvent (NGS)-MCU solvent. To support this integration of NGS into the MCU facilities, Savannah River Remediation (SRR) requested that Savannah River National Laboratory (SRNL) perform testing of a blend of the NGS (MaxCalix based solvent) with the current solvent (BOBCalixC6 based solvent) for the removal of cesium (Cs) from the liquid salt waste stream. This testing differs from prior testing by utilizing a blend of BOBCalixC6 based solvent and the NGS with the full (0.05 M) concentration of the MaxCalix as well as a new suppressor, tris(3,7dimethyloctyl) guanidine. Single stage tests were conducted using the full size V-05 and V-10 centrifugal contactors installed at SRNL. These tests were designed to determine the mass transfer and hydraulic characteristics with the NGS solvent blended with the projected heel of the BOBCalixC6 based solvent that will exist in MCU at time of transition. The test program evaluated the amount of organic carryover and the droplet size of the organic carryover phases using several analytical methods. Stage efficiency and mass distribution ratios were determined by measuring Cs concentration inmore » the aqueous and organic phases during single contactor testing. The nominal cesium distribution ratio, D(Cs) measured for extraction ranged from 37-60. The data showed greater than 96% stage efficiency for extraction. No significant differences were noted for operations at 4, 8 or 12 gpm aqueous salt simulant feed flow rates. The first scrub test (contact with weak caustic solution) yielded average scrub D(Cs) values of 3.3 to 5.2 and the second scrub test produced an average value of 1.8 to 2.3. For stripping behavior, the “first stage” D Cs) values ranged from 0.04 to 0.08. The efficiency of the low flow (0.27 gpm aqueous) was calculated to be 82.7%. The Spreadsheet Algorithm for Stagewise Solvent Extraction (SASSE) predicted equivalent DF for MCU from this testing is greater than 3,500 assuming 95% efficiency during extraction and 80% efficiency during scrub and strip. Hydraulically, the system performed very well in all tests. Target flows were easily obtained and stable throughout testing. Though some issues were encountered with plugging in the coalescer, they were not related to the solvent. No hydraulic upsets due to the solvent were experienced during any of the tests conducted. The first extraction coalescer element used in testing developed high pressure drop that made it difficult to maintain the target flow rates. Analysis showed an accumulation of sodium aluminosilicate solids. The coalescer was replaced with one from the same manufacturer’s lot and pressure drop was no longer an issue. Concentrations of Isopar™ L and Modifier were measured using semi-volatile organic analysis (SVOA) and high performance liquid chromatography (HPLC) to determine the amount of solvent carryover. For low-flow (0.27 gpm aqueous) conditions in stripping, SVOA measured the Isopar™ L post-contactor concentration to be 25 mg/L, HPLC measured 39 mg/L of Modifier. For moderate-flow (0.54 gpm aqueous) conditions, SVOA measured the Isopar™ L postcontactor to be ~69 mg/L, while the HPLC measured 56 mg/L for Modifier. For high-flow (0.8 gpm aqueous) conditions, SVOA measured the Isopar™ L post-contactor to be 39 mg/L. The post-coalescer (pre-decanter) measurements by SVOA for Isopar™ L were all less than the analysis detection limit of 10 mg/L. The HPLC measured 18, 22 and 20 mg/L Modifier for the low, medium, and high-low rates respectively. In extraction, the quantity of pre-coalescer Isopar™ L carryover measured by SVOA was ~280-410 mg/L at low flow (4 gpm aqueous), ~400-450 mg/L at moderate flow (8 gpm aqueous), and ~480 mg/L at high flow (12 gpm aqueous). The amount of post coalescer (pre-decanter) Isopar™ L carryover measured by SVOA was less than 45 mg/L for all flow rates. HPLC results for Modifier were 182, 217 and 222 mg/L for the post-contactor low, medium and high flow rates. The post-coalescer (pre-decanter) samples were measured to contain 12, 10 and 22 mg/L Modifier for the low, medium, and high flow rates. The carryover results and droplet size measurements were used to determine the decanter performance utilizing the decanter model developed by the ARES Corporation. Results show for the targeted salt flow rate of approximately 8 gpm, that over 93% of the solvent carryover from stripping is predicted to be recovered and over 96% solvent carryover from extraction is predicted to be recovered. This translates to a predicted solvent carryover of <3 ppm from stripping and <20 ppm solvent carryover from extraction. This projected performance at MCU is expected to be well within the operating limits and the historical performance for the baseline BOBCalixC6 based solvent. Droplet-size data obtained by MicroTrac™ S3400 analyzer consistently shows that the droplet size post-oalescer is significantly greater than the post-contactor or pre-coalescer samples. Increased flow rates did not show a consistent impact to the droplet size results. For the extraction testing, droplet size analysis showed that the post-contactor and pre-coalescer samples were essentially the same. The mean droplet sizes post-coalescer were less than the mean droplet sizes pre-coalescer with a very slight upward trend in the mean droplet size as the flow rate was increased. This result is probably due to the method of sampling. The larger post-coalescer drops immediately rise to the surface after leaving the coalescer element. The downstream sampling point was horizontally in-line with the element and therefore would only capture those organic droplets well mixed in the flowing aqueous stream.« less

Authors:
; ; ; ; ;
Publication Date:
Research Org.:
Savannah River Site (SRS), Aiken, SC (United States)
Sponsoring Org.:
USDOE (United States)
OSTI Identifier:
1089501
Report Number(s):
SRNL-STI-2013-00413
TRN: US1400064
DOE Contract Number:  
DE-AC09-08SR22470
Resource Type:
Technical Report
Country of Publication:
United States
Language:
English
Subject:
12 MANAGEMENT OF RADIOACTIVE AND NON-RADIOACTIVE WASTES FROM NUCLEAR FACILITIES; NGS, CSSX, cesium; solvent extraction

Citation Formats

Herman, D. T., Duignan, M. R., Williams, M. R., Peters, T. B., Poirier, M. R., and Fondeur, F. F. Mass Transfer And Hydraulic Testing Of The V-05 And V-10 Contactors With The Next Generation Solvent. United States: N. p., 2013. Web. doi:10.2172/1089501.
Herman, D. T., Duignan, M. R., Williams, M. R., Peters, T. B., Poirier, M. R., & Fondeur, F. F. Mass Transfer And Hydraulic Testing Of The V-05 And V-10 Contactors With The Next Generation Solvent. United States. https://doi.org/10.2172/1089501
Herman, D. T., Duignan, M. R., Williams, M. R., Peters, T. B., Poirier, M. R., and Fondeur, F. F. 2013. "Mass Transfer And Hydraulic Testing Of The V-05 And V-10 Contactors With The Next Generation Solvent". United States. https://doi.org/10.2172/1089501. https://www.osti.gov/servlets/purl/1089501.
@article{osti_1089501,
title = {Mass Transfer And Hydraulic Testing Of The V-05 And V-10 Contactors With The Next Generation Solvent},
author = {Herman, D. T. and Duignan, M. R. and Williams, M. R. and Peters, T. B. and Poirier, M. R. and Fondeur, F. F.},
abstractNote = {The Modular Caustic Side Solvent Extraction (CSSX) Unit (MCU) facility is actively pursuing the transition from the current BOBCalixC6 based solvent to the Next Generation Solvent (NGS)-MCU solvent. To support this integration of NGS into the MCU facilities, Savannah River Remediation (SRR) requested that Savannah River National Laboratory (SRNL) perform testing of a blend of the NGS (MaxCalix based solvent) with the current solvent (BOBCalixC6 based solvent) for the removal of cesium (Cs) from the liquid salt waste stream. This testing differs from prior testing by utilizing a blend of BOBCalixC6 based solvent and the NGS with the full (0.05 M) concentration of the MaxCalix as well as a new suppressor, tris(3,7dimethyloctyl) guanidine. Single stage tests were conducted using the full size V-05 and V-10 centrifugal contactors installed at SRNL. These tests were designed to determine the mass transfer and hydraulic characteristics with the NGS solvent blended with the projected heel of the BOBCalixC6 based solvent that will exist in MCU at time of transition. The test program evaluated the amount of organic carryover and the droplet size of the organic carryover phases using several analytical methods. Stage efficiency and mass distribution ratios were determined by measuring Cs concentration in the aqueous and organic phases during single contactor testing. The nominal cesium distribution ratio, D(Cs) measured for extraction ranged from 37-60. The data showed greater than 96% stage efficiency for extraction. No significant differences were noted for operations at 4, 8 or 12 gpm aqueous salt simulant feed flow rates. The first scrub test (contact with weak caustic solution) yielded average scrub D(Cs) values of 3.3 to 5.2 and the second scrub test produced an average value of 1.8 to 2.3. For stripping behavior, the “first stage” D Cs) values ranged from 0.04 to 0.08. The efficiency of the low flow (0.27 gpm aqueous) was calculated to be 82.7%. The Spreadsheet Algorithm for Stagewise Solvent Extraction (SASSE) predicted equivalent DF for MCU from this testing is greater than 3,500 assuming 95% efficiency during extraction and 80% efficiency during scrub and strip. Hydraulically, the system performed very well in all tests. Target flows were easily obtained and stable throughout testing. Though some issues were encountered with plugging in the coalescer, they were not related to the solvent. No hydraulic upsets due to the solvent were experienced during any of the tests conducted. The first extraction coalescer element used in testing developed high pressure drop that made it difficult to maintain the target flow rates. Analysis showed an accumulation of sodium aluminosilicate solids. The coalescer was replaced with one from the same manufacturer’s lot and pressure drop was no longer an issue. Concentrations of Isopar™ L and Modifier were measured using semi-volatile organic analysis (SVOA) and high performance liquid chromatography (HPLC) to determine the amount of solvent carryover. For low-flow (0.27 gpm aqueous) conditions in stripping, SVOA measured the Isopar™ L post-contactor concentration to be 25 mg/L, HPLC measured 39 mg/L of Modifier. For moderate-flow (0.54 gpm aqueous) conditions, SVOA measured the Isopar™ L postcontactor to be ~69 mg/L, while the HPLC measured 56 mg/L for Modifier. For high-flow (0.8 gpm aqueous) conditions, SVOA measured the Isopar™ L post-contactor to be 39 mg/L. The post-coalescer (pre-decanter) measurements by SVOA for Isopar™ L were all less than the analysis detection limit of 10 mg/L. The HPLC measured 18, 22 and 20 mg/L Modifier for the low, medium, and high-low rates respectively. In extraction, the quantity of pre-coalescer Isopar™ L carryover measured by SVOA was ~280-410 mg/L at low flow (4 gpm aqueous), ~400-450 mg/L at moderate flow (8 gpm aqueous), and ~480 mg/L at high flow (12 gpm aqueous). The amount of post coalescer (pre-decanter) Isopar™ L carryover measured by SVOA was less than 45 mg/L for all flow rates. HPLC results for Modifier were 182, 217 and 222 mg/L for the post-contactor low, medium and high flow rates. The post-coalescer (pre-decanter) samples were measured to contain 12, 10 and 22 mg/L Modifier for the low, medium, and high flow rates. The carryover results and droplet size measurements were used to determine the decanter performance utilizing the decanter model developed by the ARES Corporation. Results show for the targeted salt flow rate of approximately 8 gpm, that over 93% of the solvent carryover from stripping is predicted to be recovered and over 96% solvent carryover from extraction is predicted to be recovered. This translates to a predicted solvent carryover of <3 ppm from stripping and <20 ppm solvent carryover from extraction. This projected performance at MCU is expected to be well within the operating limits and the historical performance for the baseline BOBCalixC6 based solvent. Droplet-size data obtained by MicroTrac™ S3400 analyzer consistently shows that the droplet size post-oalescer is significantly greater than the post-contactor or pre-coalescer samples. Increased flow rates did not show a consistent impact to the droplet size results. For the extraction testing, droplet size analysis showed that the post-contactor and pre-coalescer samples were essentially the same. The mean droplet sizes post-coalescer were less than the mean droplet sizes pre-coalescer with a very slight upward trend in the mean droplet size as the flow rate was increased. This result is probably due to the method of sampling. The larger post-coalescer drops immediately rise to the surface after leaving the coalescer element. The downstream sampling point was horizontally in-line with the element and therefore would only capture those organic droplets well mixed in the flowing aqueous stream.},
doi = {10.2172/1089501},
url = {https://www.osti.gov/biblio/1089501}, journal = {},
number = ,
volume = ,
place = {United States},
year = {Wed Jul 31 00:00:00 EDT 2013},
month = {Wed Jul 31 00:00:00 EDT 2013}
}