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Title: Demonstration of a fuel-saving system for paint-curing ovens

Technical Report ·
DOI:https://doi.org/10.2172/6658015· OSTI ID:6658015

Two curing ovens at Roll Coater, Inc. (the Greenfield, Indiana plant) were retrofitted to save fuel and cost. Included in the fuel conserving retrofit was the design, fabrication, and installation of an afterburner for each of the two ovens, piping their combustion products to each of two commonly housed waste heat boilers before discharge from those units to the atmosphere at about 450 F. Depending on the product being run and the coating applied, natural gas requirements have been reduced by 45 to 65% with operation of the zone incinerators only and by as much as 65 to 85% including the effects of both the zone incineration and heat recovery by means of the afterburners and waste heat boilers. A demonstration program on conversion work at the No. 3 line at Greenfield and results are described in Section 2. Section 3 describes the retrofit design and the system construction. System performance (tests and measurements, qualitative performance, maintenance factors, and economic performance) is described in Section 4. Conclusions and recommendations are summarized.

Research Organization:
EG and G Idaho, Inc., Idaho Falls, ID (United States)
DOE Contract Number:
AC07-76CS40009
OSTI ID:
6658015
Report Number(s):
DOE/CS/40009-T1
Resource Relation:
Other Information: Portions of document are illegible
Country of Publication:
United States
Language:
English