High SO{sub 2} removal efficiency testing: Evaluation of high efficiency test results at Hoosier Energy`s Merom Station
Tests were conducted at Hoosier Energy`s Merom Station 535-MW Units 1 and 2 wet limestone flue gas desulfurization (FGD) systems to evaluate options for achieving high SO{sub 2} removal efficiency. The options tested included use of dibasic acid (DBA) and sodium formate additives as well as operation at higher reagent ratios (higher pH set points). In addition to the tested options, the effectiveness of other potential options was simulated using the Electric Power Research Institute`s FGD Process Integration and Simulation Model (FGDPRISM) after it was calibrated to the system. An economic analysis was done to determine the cost effectiveness of each option. A summary of results is given on the following: SO{sub 2} removal performance; additive consumption; and SO{sub 2} removal upgrade economics.
- Research Organization:
- Radian Corp., Austin, TX (United States)
- Sponsoring Organization:
- USDOE Assistant Secretary for Fossil Energy, Washington, DC (United States)
- DOE Contract Number:
- AC22-92PC91338
- OSTI ID:
- 481948
- Report Number(s):
- DOE/PC/91338-T24; ON: DE97052397; TRN: AHC29712%%11
- Resource Relation:
- Other Information: PBD: 22 Apr 1996
- Country of Publication:
- United States
- Language:
- English
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