Innovative Clean Coal Technology (ICCT): 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. Technical progress report, Fourth quarter 1992
This quarterly report discusses the technical progress of an Innovative Clean Coal Technology (ICCT) demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. The primary goal of this project is the characterization of the low NO{sub x} combustion equipment through the collection and analysis of long-term emissions data. A target of achieving fifty percent NO{sub x} reduction using combustion modifications has been established for the project. The project provides a stepwise retrofit of an advanced overfire air (AOFA) system followed by low NO{sub x} burners (LNB). During each test phase of the project, diagnostic, performance, long-term, and verification testing will be performed. These tests are used to quantify the NO{sub x } reductions of each technology and evaluate the effects of those reductions on other combustion parameters such as particulate characteristics and boiler efficiency. Baseline, AOFA, and LNB without AOFA test segments have been completed. Analysis of the 94 days of LNB tong-term data collected show the full load NO{sub x} emission levels to be approximately 0.65 lb/MBtu. Flyash LOI values for the LNB configuration are approximately 8 percent at full load. Corresponding values for the AOFA configuration are 0.94 lb/MBtu and approximately 10 percent. Abbreviated diagnostic tests for the LNB+AOFA configuration indicate that at 500 MWe, NO{sub x} emissions are approximately 0.55 lb/MBtu with corresponding flyash LOI values of approximately 11 percent. For comparison, the long-term, full load, baseline NO{sub x} emission level was approximately 1.24 lb/MBtu at 5.2 percent LOI. Comprehensive testing of the LNB+AOFA configuration will be performed when the stack particulate emissions issue is resolved.
- Research Organization:
- Southern Co. Services, Inc., Birmingham, AL (United States)
- Sponsoring Organization:
- USDOE, Washington, DC (United States)
- DOE Contract Number:
- FC22-90PC89651
- OSTI ID:
- 10191632
- Report Number(s):
- DOE/PC/89651-T9; ON: DE94001971; BR: AZ0404010
- Resource Relation:
- Other Information: PBD: [1992]
- Country of Publication:
- United States
- Language:
- English
Similar Records
Innovative Clean Coal Technology (ICCT): 500 MW demonstration of advanced wall-fired combustion techniques for the reduction of nitrogen oxide (NO{sub x}) emissions from coal-fired boilers. Third quarterly technical progress report
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Related Subjects
01 COAL, LIGNITE, AND PEAT
FOSSIL-FUEL POWER PLANTS
AIR POLLUTION CONTROL
NITROGEN OXIDES
PERFORMANCE TESTING
COAL
STAGED COMBUSTION
US CLEAN COAL TECHNOLOGY PROGRAM
DEMONSTRATION PROGRAMS
PROGRESS REPORT
BOILERS
EMISSION
RETROFITTING
EXPERIMENTAL DATA
200202
010800
NOXIOUS GAS AND PARTICULATE EMISSIONS
WASTE MANAGEMENT