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Title: Development and testing of a high efficiency advanced coal combustor phase III industrial boiler retrofit. Quarterly technical progress report No. 9, 1 October 1993--31 December 1993

Technical Report ·
DOI:https://doi.org/10.2172/10156873· OSTI ID:10156873
;  [1]; ;  [2];  [3]
  1. ABB/Combustion Engineering, Windsor, CT (United States)
  2. Penn State Univ., University Park, PA (United States)
  3. Univ. of Massachusetts, Amherst, MA (United States)

This report documents the technical aspects of this project during the ninth quarter of the program. During this quarter, the natural gas baseline testing at the Penn State demonstration boiler was completed, results were analyzed and are presented here. The burner operates in a stable manner over an 8/1 turndown, however due to baghouse temperature limitations (300{degrees}F for acid dewpoint), the burner is not operated for long periods of time below 75% load. Boiler efficiency averaged 83.1% at the 100 percent load rate while increasing to 83.7% at 75% load. NO{sub x} emissions ranged from a low of 0.17 Lbs/MBtu to a high of 0.24 Lbs/MBtu. After the baseline natural gas testing was completed, work continued on hardware optimization and testing with the goal of increasing carbon conversion efficiency on 100% coal firing from {approx}95% to 98%. Several coal handling and feeding problems were encountered during this quarter and no long term testing was conducted. While resolving these problems several shorter term (less than 6 hour) tests were conducted. These included, 100% coal firing tests, 100% natural gas firing tests, testing of air sparges on coal to simulate more primary air and a series of cofiring tests. For 100% coal firing, the carbon conversion efficiency (CCE) obtained this quarter did not exceed the 95-96% barrier previously reached. NO{sub x} emissions on coal only ranged from {approx} 0.42 to {approx} 0.78 Lbs/MBtu. The burner has not been optimized for low NO{sub x} yet, however, due to the short furnace residence time, meeting the goals of 98% CCE and <0.6 Lbs/MBtu NO{sub x} simultaneously will be difficult. Testing on 100% natural gas in the boiler after coal firing indicated no changes in efficiency due to firing in a `dirty` boiler. The co-firing tests showed that increased levels of natural gas firing proportionately decreased NO{sub x}, SO{sub 2}, and CO.

Research Organization:
ABB Combustion Engineering, Inc., Windsor, CT (United States). ABB Power Plant Labs.
Sponsoring Organization:
USDOE, Washington, DC (United States)
DOE Contract Number:
AC22-91PC91160
OSTI ID:
10156873
Report Number(s):
DOE/PC/91160-T2; ON: DE94013055; IN: PPL-94-CR-2; TRN: 94:006045
Resource Relation:
Other Information: PBD: 1 Mar 1994
Country of Publication:
United States
Language:
English