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Title: Demonstration of selective catalytic reduction technology for the control of nitrogen oxide emissions from high-sulfur, coal-fired boilers

Conference ·
OSTI ID:10103739

This paper describes the status of the Innovative Clean Coal Technology project to demonstrate SCR technology for reduction of NO{sub x} emissions from flue gas of utility boilers burning US high-sulfur coal. The funding participants are the US Department of Energy (DOE), Southern Company Services, Inc. (SCS), on behalf of the entire Southern Company, Electric Power Research Institute (EPRI), and Ontario Hydro. SCS is the participant responsible for managing all aspects of the project. The project is being conducted on Gulf Power Company`s Plant Crist Unit 5 (75-MW nominal capacity), located near Pensacola, Florida, on US coals that have a sulfur content near 3.0%. The SCR facility treats a 17,400 scfm slip-stream of flue gas and consists of three 2.5-MW (5000 scfm) and six 0.2-MW (400 scfm) SCR reactors. The reactors operate in parallel with commercially available SCR catalysts obtained from vendors throughout the world. The design engineering and construction have been completed, and the startup/shakedown was completed in June 1993. Long-term performance testing began in July 1993 and will be conducted for two years. Test facility description and test plans, as well as start-up issues and preliminary commissioning test results are reported in this paper.

Research Organization:
Southern Co. Services, Inc., Birmingham, AL (United States)
Sponsoring Organization:
USDOE, Washington, DC (United States)
DOE Contract Number:
FC22-90PC89652
OSTI ID:
10103739
Report Number(s):
CONF-9309152-3; ON: DE94001960; BR: AZ0404020
Resource Relation:
Conference: 2. annual clean coal technology conference,Atlanta, GA (United States),7-9 Sep 1993; Other Information: PBD: [1993]
Country of Publication:
United States
Language:
English