Coiled tubing facilitates deep underbalanced workover
Journal Article
·
· Oil and Gas Journal
OSTI ID:462703
- Chevron USA Production Co., Midland, TX (United States)
- CUDD Pressure Control Inc., Houston, TX (United States)
A recent workover shows the technical capability and cost effectiveness of coiled tubing for cleaning out scale in a 22,611-ft, low pressure, high-temperature gas well. The well, operated by Chevron USA Production Co., is in the Fort Stockton Gas Unit 5-1 Gomez (Ellenburger) field, in West Texas. The development of reliable 100,000-psi minimal yield strength coiled tubing was a major factor that allowed this work to succeed. The methods demonstrated by this workover are becoming a standard for deep well cleanouts in the Gomez (Ellenburger) field. The paper describes coiled tubing advantages, well history, and implementation.
- OSTI ID:
- 462703
- Journal Information:
- Oil and Gas Journal, Vol. 95, Issue 13; Other Information: PBD: 31 Mar 1997
- Country of Publication:
- United States
- Language:
- English
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