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Title: Increasing positive displacement charging pump reliability

Conference ·
OSTI ID:268106
 [1]
  1. Entergy Operations, Inc., Killona, LA (United States)

The use of positive displacement pumps in many PWRs is an integral part of providing reactivity control via the Chemical and Volume Control system. This usually requires the continuous operation of at least one pump, typically with a flow rate of 44 gpm {at} 2,310 psig (167 lpm {at} 160 bar). Some PWRs use multiple pumps, and vary the letdown, while others use variable speed pumps. Regardless, the charging pumps run continuously. With the amount of reciprocating mass, differential pressure, and friction, it is a battle to maintain the pumps in peak operating condition for long periods of time. This paper will show how Entergy Operations` Waterford 3 SES was able to increase the reliability of the positive displacement Charging Pumps. Many different solutions were evaluated, and several adopted. The results are undeniable, as availability has increased and O and M costs have been reduced by 90% over 6 years.

OSTI ID:
268106
Report Number(s):
CONF-960306-; ISBN 0-7918-1226-X; TRN: 96:016738
Resource Relation:
Conference: ICONE 4: ASME/JSME international conference on nuclear engineering, New Orleans, LA (United States), 10-13 Mar 1996; Other Information: PBD: 1996; Related Information: Is Part Of ICONE-4: Proceedings. Volume 4: Nuclear plant operations and maintenance, nuclear fuel cycle, institutional and energy policy, non-proliferation and safeguards; Rao, A.S. [ed.] [General Electric Nuclear Energy, San Jose, CA (United States)]; Duffey, R.B. [ed.] [Brookhaven National Lab., Upton, NY (United States)]; Elias, D. [ed.] [Commonwealth Edison, Downers Grove, IL (United States)]; PB: 745 p.
Country of Publication:
United States
Language:
English