Recent Process and Equipment Improvements to Increase High Level Waste Throughput at The Defense Waste Processing Facility (DWPF)
Abstract
The Savannah River Site's (SRS) Defense Waste Processing Facility (DWPF) began stabilizing high level waste (HLW) in a glass matrix in 1996. Over the past few years, there have been several process and equipment improvements at the DWPF to increase the rate at which the high level waste can be stabilized. These improvements have either directly increased waste processing rates or have desensitized the process to upsets, thereby minimizing downtime and increasing production. Improvements due to optimization of waste throughput with increased HLW loading of the glass resulted in an 8 % waste throughput increase over the standard 28 % waste loading based upon operational efficiencies. Improvements in canister production include the pour spout heated bellows liner (7 %), glass surge (siphon) protection software (2 %), melter feed pump software logic change to prevent spurious interlocks of the feed pump with subsequent dilution of feed stock (2 %) and optimization of the steam atomized scrubber (SAS) operation to minimize downtime (3 %) for a total increase in canister production of 14 %. A number of process recovery efforts have allowed continued operation. These include the off gas system pluggage and restoration, slurry mix evaporator (SME) tank repair and replacement, remotemore »
- Authors:
-
- Defense Waste Processing Facility, Washington Savannah River Co. (WSRC), Aiken, SC (United States)
- Publication Date:
- Research Org.:
- WM Symposia, 1628 E. Southern Avenue, Suite 9 - 332, Tempe, AZ 85282 (United States)
- OSTI Identifier:
- 21323114
- Report Number(s):
- INIS-US-10-WM-08366
TRN: US10V0566064305
- Resource Type:
- Conference
- Resource Relation:
- Conference: WM'08: Waste Management Symposium 2008 - HLW, TRU, LLW/ILW, Mixed, Hazardous Wastes and Environmental Management - Phoenix Rising: Moving Forward in Waste Management, Phoenix, AZ (United States), 24-28 Feb 2008; Other Information: Country of input: France; 9 refs
- Country of Publication:
- United States
- Language:
- English
- Subject:
- 12 MANAGEMENT OF RADIOACTIVE WASTES, AND NON-RADIOACTIVE WASTES FROM NUCLEAR FACILITIES; HIGH-LEVEL RADIOACTIVE WASTES; OFF-GAS SYSTEMS; RADIOACTIVE WASTE FACILITIES; RADIOACTIVE WASTE PROCESSING; SAVANNAH RIVER PLANT; SLURRIES; WASTE PROCESSING PLANTS
Citation Formats
O'Driscoll, R J, Barnes, A B, Coleman, J R, Glover, T L, Hopkins, R C, Iverson, D C, and Leita, J N. Recent Process and Equipment Improvements to Increase High Level Waste Throughput at The Defense Waste Processing Facility (DWPF). United States: N. p., 2008.
Web.
O'Driscoll, R J, Barnes, A B, Coleman, J R, Glover, T L, Hopkins, R C, Iverson, D C, & Leita, J N. Recent Process and Equipment Improvements to Increase High Level Waste Throughput at The Defense Waste Processing Facility (DWPF). United States.
O'Driscoll, R J, Barnes, A B, Coleman, J R, Glover, T L, Hopkins, R C, Iverson, D C, and Leita, J N. 2008.
"Recent Process and Equipment Improvements to Increase High Level Waste Throughput at The Defense Waste Processing Facility (DWPF)". United States.
@article{osti_21323114,
title = {Recent Process and Equipment Improvements to Increase High Level Waste Throughput at The Defense Waste Processing Facility (DWPF)},
author = {O'Driscoll, R J and Barnes, A B and Coleman, J R and Glover, T L and Hopkins, R C and Iverson, D C and Leita, J N},
abstractNote = {The Savannah River Site's (SRS) Defense Waste Processing Facility (DWPF) began stabilizing high level waste (HLW) in a glass matrix in 1996. Over the past few years, there have been several process and equipment improvements at the DWPF to increase the rate at which the high level waste can be stabilized. These improvements have either directly increased waste processing rates or have desensitized the process to upsets, thereby minimizing downtime and increasing production. Improvements due to optimization of waste throughput with increased HLW loading of the glass resulted in an 8 % waste throughput increase over the standard 28 % waste loading based upon operational efficiencies. Improvements in canister production include the pour spout heated bellows liner (7 %), glass surge (siphon) protection software (2 %), melter feed pump software logic change to prevent spurious interlocks of the feed pump with subsequent dilution of feed stock (2 %) and optimization of the steam atomized scrubber (SAS) operation to minimize downtime (3 %) for a total increase in canister production of 14 %. A number of process recovery efforts have allowed continued operation. These include the off gas system pluggage and restoration, slurry mix evaporator (SME) tank repair and replacement, remote cleaning of melter top head center nozzle, remote melter internal inspection, SAS pump J-Tube recovery, inadvertent pour scenario resolutions, dome heater transformer bus bar cooling water leak repair and new Infra-red camera for determination of glass height in the canister are discussed. (authors)},
doi = {},
url = {https://www.osti.gov/biblio/21323114},
journal = {},
number = ,
volume = ,
place = {United States},
year = {Tue Jul 01 00:00:00 EDT 2008},
month = {Tue Jul 01 00:00:00 EDT 2008}
}