Low-level liquid waste treatment system start-up
Following removal of Cs-137 by ion exchange in the Supernatant Treatment System immediately upstream, the radioactive liquid waste is volume-reduced by evaporation. Trace amounts of Cs-137 in the resulting distillate are removed by ion exchange, then the distillate is discharged to the existing plant water treatment system. The concentrated product, 37 to 41 percent solids (by weight), is encapsulated in cement, producing a stable low-level waste form. This report provides a summary of work performed to test the Liquid Waste Treatment System following construction turnover and prior to radioactive operation. All mechanical and electrical components, piping, valves, pumps, tanks, controls, and instrumentation required to operate the system were tested; first with water, then with simulated waste. Subsystems (individual tanks, pumps, and control loops) were tested individually, then as a complete system. Finally, the system began a controlled start-up phase, which included the first four months of radioactive operation. Components were tested for operability then for performance data to verify the system`s ability to produce an acceptable waste form at design feed rates.
- Research Organization:
- West Valley Nuclear Services Co., Inc., West Valley, NY (United States)
- Sponsoring Organization:
- USDOE, Washington, DC (United States)
- DOE Contract Number:
- AC07-81NE44139
- OSTI ID:
- 10197011
- Report Number(s):
- DOE/NE/44139-55; ON: DE95004254
- Resource Relation:
- Other Information: PBD: Jul 1989
- Country of Publication:
- United States
- Language:
- English
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